11 September 2015 | HOME - Vancouver WA
24 August 2015 | 46 11.4'N:123 51.4'W, Port of Astoria Marina
22 August 2015 | 46 42.0'N:132 09,4'W, 330 West of CR Bouy, Astoria
21 August 2015 | 46 41.8'N:136 13.8'W, 500 West of Astoria
20 August 2015 | 46 22.82'N:140 28.00'W, East end of High
20 August 2015 | 46 22.80'N:140 28.32'W, Middle of High Same as Fish
20 August 2015 | 46 22.79'N:140 28.57'W, Middle of High
20 August 2015 | 46 22.7'N:140 30.2'W, 675 Miles West of CR
20 August 2015 | 45 57.6'N:144 54.0'W, East End of the High
18 August 2015 | 44 38.2'N:147 57.0'W, 1000 NM to Astoria
18 August 2015 | 43 31.0'N:150 28.0'W, 1126 NM to Astoria
17 August 2015 | 41 40.1'N:153 00.1'W, 1200 miles West of Astoria
16 August 2015 | 39 30.1'N:154 53.1'W, West end of the North Pacific High
15 August 2015 | 37 34.5'N:156 00.0'W, 1011 North of Oahu
15 August 2015 | 37 04.5'N:156 23.0'W, 983 North of Oahu
14 August 2015 | 34 12.3'N:157 26.1'W, 800 North of Oahu
13 August 2015 | 31 50.0'N:158 06.5'W, 650 North of Oahu
12 August 2015 | 29 02.0'N:158 51.0'W, 330 North of Oahu
11 August 2015 | 26 32.0'N:158 59.0'W, 330 North of Oahu
09 August 2015 | 23 44.1'N:158 49.4'W, 140 N of Oahu
Steering Gone Bad
20 August 2015 | 45 57.6'N:144 54.0'W, East End of the High
John
Steering Gone Bad
At 1830Z we change from Port to Starboard engine. In the porcess the autopilot
kicked off. I tried to steer by hand and it was very hard. My first
assumption was that we snagged some garbage on one of the rudders and it
wouldn't let me steer. Thought I was going to have to go into the water.
Opened up the port engine hatch and discovered the rudder quadrant post that
connects the autopilot ram and the cross arm to the quadarant had sheered and
was jammed under the quadrant. I knew I had a spare quadrant and didn't know
why. It also looked as if it was used like it had been on one of the rudder
posts before. So it is highly likely that the pinion post is not substantial
enough. Fortunately the starboard side has the same pinion post because I
didn't have a spare one. I removed the pinion from the starboard side and
found a bolt and nut to replace the starboard pinion. Trouble is the whole on
the ball joint was about 5/8" in diameter and the bolt that would work was only
a 3/8. I needed a bushing. Remembering I had a small sheet of brass thin
plate, I was going to cut a strip about 3/4" wide and twist it up into a
bushing to take out the slop from the two different sized objects. As luck
would have it I happened to have a bronze hose barb fitting that was for a 5/8"
hose and the inside was exactly 3/8". Cut the barb off and there was the
bushing. We also could not get the rudder angle sensor post off the old
quadrant so I had to dig into my spare autopilot kit and salvage one from
there. All in all it took just under 2 hours to make the repair. I will check
it daily for any signs of wear. I sure don't want to have to hand steer for 5
days.
After we finished up the work on the rudder quadrant we got back underway.
Mosese and Malo transfered fuel from 7 of the jerries into the Port tank while
I replaced the first stage filter on the water maker. It was so bad I couldn't
even clean it, had to just replace it. Our previous water maker by Village
Marine used a single 20 micron sea water filter to feed the membranes. My new
water maker by RO uses 2 filters, a 20 micron and a 5 micron. RO says the
membranse will last for years. Village says they need to be replace after so
many years or when the volume decreases by so much. Village with the single
filter is allowing some stuff smaller than 20 microns to coat the membranes
wheras RO only lets stuff smaller than 5 microns in. There was a definate
discolleration on the 5 micron filter but surely not enough to change it. Time
will tell. When we get home I will have to pickle the system and put a
chemical in it to preserve the membranes.
Fuel use has been low but we definately need to use up what we are carrying on
deck before we get to Astoria or at least by the time we get home. We were
carrying 660 liters on deck along with the 640 in the tanks. So far only used
175 and change. We have been motoring for the past 36 hours and will have at
least another 24 to 30 before we see any substantial wind going our way.
I got an email back from Bob and Ann on Charisma telling me they were rolling
on the floor, dying with laughter reading yesterday's blog. I presume that
means they might not rely on their bread too much.
As the day progressed we made some necessary repairs to essential halyards,
reefers and the such. The main halyard has a 2:1 turnng block at the head of
the sail that has a special shackel to clip onto the sail but it is not
metaliclly affixed to the block. It had to be attached using some strapping.
It had shown some signs of wear and tear gefore we left HI but I thought it
might make it home. NOT! It was near giving away. Reomoved the web stap and
laced it together using some Dynema. Not pretty but damn functional. The we
replace the furling line for the main, as the old one was showing signs of
parting somewhere very inconvenient. Found some older line and and replace the
furling line then lashed the turning block at the base of the mast that was the
cause of the chaffing.
Wind is back up to 8-10kts on the beam, sails are back up, one reef in the main
and full gib. Motor sailing at 7.5 knots heading for the barn. If the speed
and seas continu the way they are we are 5 days out of Astoria.
All for now.
John